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One-In-Three Chance Of US
Nuclear Reactor Accident
By Garry Lenton
The Patriot-News
9-4-3

More than half of the nation's nuclear power plants have been told to correct a design flaw that federal researchers believe increases the risk of an accident.
 
The concern is that water bursting under extremely high pressure from a ruptured pipe inside the building that houses the reactor could churn up enough debris to clog sump pumps designed to return the water to the reactor's cooling system.
 
If that happened, the risk that control room operators would not be able to keep the reactor cool increases by a factor of 10, according to a study conducted at the Los Alamos National Laboratory. Nuclear reactors, like car engines, can be severely damaged if allowed to overheat.
 
Researchers are concerned that the design flaw could lead to accidents like the one that destroyed the Unit 2 reactor at Three Mile Island in 1979.
 
According to the Union of Concerned Scientists, a watchdog group, the Los Alamos study reports that debris blockage would raise the probability of an accident at TMI from one in 67,000 years to one in 432 to 536 years.
 
During the 1979 accident at the Londonderry Twp. plant, operators failed to realize that a release valve jammed open, allowing water and steam to leak out of the cooling system. The error resulted in a partial meltdown of the reactor fuel and the release of radiation into the air.
 
In a bulletin issued in June to the owners of 69 of the nation's 104 nuclear plants, including TMI and Beaver Valley in Shippingport, Beaver County, the U.S. Nuclear Regulatory Commission called on plant owners to assess their plants' vulnerability and take corrective measures.
 
The changes could range from installing larger filtering screens around the pumps to training operators how to manipulate water flows to dislodge clogs, said Scott Burnell, a spokesman for the agency.
 
Officials at Exelon Nuclear, part owner of TMI, said they have determined that the plant is not at high risk.
 
The problem affects the largest class of nuclear reactors in use in the country -- pressurized water reactors, or PWRs. The other class, boiling water reactors, identified and fixed the problem in the 1990s. The NRC only recently concluded that PWRs were also vulnerable to the problem.
 
But fixing the PWRs will not be as easy because their designs are more varied, said John Butler, senior project manager of risk regulations for The Nuclear Energy Institute, an industry group.
 
"You can't easily identify a single solution that will fix it for everyone," Butler said. "It's not even easy to identify whether or not it's a problem for an individual plant."
 
The cost of the upgrading the plants could run from several hundred thousand dollars into the millions, Butler said.
 
Plant operators must shut down their plants to make the changes. Commercial nuclear plants shut down for maintenance and refueling every two years. Some may not be able to complete the work during one outage.
 
TMI is scheduled to shut down for refueling in October. At that time, workers will inspect the building for dirt, dust and small debris, said Ralph DeSantis, a spokesman for the energy company.
 
TMI is not a high-risk plant because its piping, valves and other hardware are separated from the sump pumps by a concrete wall 3 to 4 feet thick.
 
Water reaches the sump pump through a series of drains, DeSantis said. "We do inspections after outages to make sure there is no foreign material where it shouldn't be," he said.
 
The Union of Concerned Scientists has been prodding the NRC to move faster to correct the design flaws. UCS director David Lochbaum was critical of the agency's decision to give plant operators until 2007 to make changes.
 
In a recent statement, he accused the agency of "virtually ignoring" the issue and choosing instead to focus its attention on the financial performance of the nuclear industry.
 
"According to the NRC's data, there's about a 34 percent chance that one of the ... [reactors] will experience core damage between now and the time that the agency intends to fix the containment sump issue," he wrote.
 
Lochbaum also took issue with an NRC recommendation that plants shut down backup pump systems that would delay the start of the main sump system.
 
"Many of the proposed interim measures can actually increase risk quite substantially," Lochbaum wrote in a letter to NRC Chairman Nils J. Diaz.
 
The Nuclear Energy Institute shared Lochbaum's concerns.
 
Butler said the group warned its members to take a broad view of the situation to ensure that the change "would not have a detrimental effect on other events."
 
The NRC's Burnell said the agency never advocated taking actions that would adversely affect the safety of the plants.
 
"We fully expect the licensees will do detailed analysis of what actions they expect to take [and] that in doing one thing they don't make another thing worse," he said.
 
GARRY LENTON: 255-8264 or glenton@patriot-news.com
 
 
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